Surprised the wifey this morning. Maybe 6 months ago she had picked out a set of wheels for this thing. Last week i ordered them, and successfully got her tires mounted and balanced on em without her knowing. Set the toe real quick... ...and slapped em on! Its gonna need flares to pass PA inspection... ...and the money shot Took some measurements, and it ended up right at 4" lift. Nailed it! Ive still got some loose ends to button up under the hood, but im hoping to have it running in another week or so... From there it was just a matter of putting the motor back together! After cleaning the throttle body and replacing the EGR & IAC, the plenum went back on New cap, rotor, ford racing 9mm wires, and a MSD ignition coil ...and i think thats it? This week coming up i need to replace the a/c condenser (i punctured it by accident), which means conversion to R134a. Then radiator, plumb trans cooler, fuel tank + pump & filter, and then i think i can finally try to get it running! So, i made some progress on the 90 bronco. Stripped the motor down and changed the timing chain The smog pump is shot along with all the air pipes, so its all going away Its not easy to see, but they bolt to the back of the head The holes are threaded, because when flipped to the other side of the motor a threaded insert goes in it, and the accessory drive bolts to it. Which means we can plug the hole simply by putting a short bolt in it. No smog pump means no TAD or TAB, so the vacuum system came off for repairs and the removal of about half the vacuum lines pulled the plenum and then pulled the fuel rail so i could clean and then rebuild the fuel injectors i changed the rusty (but otherwise apparently in good shape) spark plugs The IAT was super gross so that got changed, along with the ECT since i was already in there So in the process of the rebuild, i decided to get rid of the fire hazard that is the 2g alt Just a small amount of grinding on this web, and the 3g alt fits right in there bracket cleaned up & installed; reman alt installed as well: I also tossed the junk Ford steering pump in favor of a Saginaw off an Econoline bracket all cleaned up, with reman pump installed and i deleted the OEM cooling loop on the frame rail in favor of a proper steering cooler off of a Superduty: |
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